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Defect reduction in an electrical parts manufacturer: a case study

Raja Sreedharan V. (Department of Management, Amrita Vishwa Vidyapeetham, Kochi, India)
Rajasekar S. (Department of Industrial Engineering, CEG, Anna University, Chennai, India)
Santhosh Kannan S. (Department of Management, Amrita Vishwa Vidyapeetham, Kochi, India)
Arunprasad P. (Dubai Business School, University of Dubai, Dubai, United Arab Emirates)
Rajeev Trehan (Department of Industrial and Production Engineering, Center of Training and Placement, Dr. B.R. Ambedkar National Institute of Technology, Jalandhar, India)

The TQM Journal

ISSN: 1754-2731

Article publication date: 11 September 2018

Issue publication date: 24 September 2018

837

Abstract

Purpose

Defective parts in manufacturing is a serious issue faced by every manufacturer. Even after proper care in design, material selection and manufacturing of product, there exists a defective part. The purpose of this paper is to explore the quality of the manufacturing, and find the use of effective quality tools to reduce the part defect rate in an electrical parts manufacturing unit, thereby, reducing the replaced cost of defective parts.

Design/methodology/approach

With the help of quality initiatives, like total quality management (TQM) and Lean Six Sigma (LSS), the firms can produce quality product in each stage of production. The paper focuses on the primary data collected from the XYZ electric manufacturer.

Findings

The main finding of this case analysis is that by the effective use of quality tools, the defective part return rate can be reduced, because of which the firm can observe reduction in replaced cost of almost INR24 lakh. In addition, 10A switch part contributes more in replacement cost. Further, it adds to the 35 percent of the overall part rejection.

Research limitations/implications

The study is more focused on particular type of switch product and can extend to other types of products. In addition, the analysis reveals the results of only 88 percent of the defective products.

Practical implications

The study provides results of the improved quality by effective use of quality tools and discusses the different types of defects in the electrical parts manufacturing. Introducing TQM and LSS to manufacturing can reduce the customer return rate to 1,300 parts per million (PPM) and even to 1,000 PPM in future.

Originality/value

The paper discusses the quality issues in the electrical manufacturer. Moreover, the case analysis briefs effective ways to improve the product quality and reduce the rejection rate.

Keywords

Citation

Sreedharan V., R., S., R., Kannan S., S., P., A. and Trehan, R. (2018), "Defect reduction in an electrical parts manufacturer: a case study", The TQM Journal, Vol. 30 No. 6, pp. 650-678. https://doi.org/10.1108/TQM-03-2018-0031

Publisher

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Emerald Publishing Limited

Copyright © 2018, Emerald Publishing Limited

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